side view of the robot with the wheel on top to access the lock. what worked well was the track as it was able to move the robot left, right, forward and backwards. the structure was very well built but the only downfall was that the wheel was to high on the robot.
Why we chose to change the bot was because we immediately noticed that the tire on the lock kept on moving and wouldn't stay still on the the lock. So to solve the problem we made the tire lower to it could directly touch the side of the lock for maximum spinning power
Why we chose to change the bot was because we immediately noticed that the tire on the lock kept on moving and wouldn't stay still on the the lock. So to solve the problem we made the tire lower to it could directly touch the side of the lock for maximum spinning power